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My GEMS Story (TVR Sprint Magazine Article)



My GEMS Story

From the moment I first climbed into my beloved Chimaera on a freezing winter’s night in 2006 I had already visualised its future. Setting off from the home of the (visibly upset) former owner onto a pitch-black motorway with the ice warning light emblazoned before me, worrying that I had just bought far too much car for my level of driving experience, when I really should have been thinking about simply enjoying my new car; I confess that at this point I was already plotting my first modification. I am going to take the time right now to place the blame for this squarely on one person: Mr. Chris Manley.
Unfortunately for me, Chris was and still is very good friends with Tim Lamont of ACT and even more unfortunately around 2004, had recently sold his S3 and bought Tim’s own highly modified pre-cat Griffith – a lovely car that he still owns today. One evening Chris kindly invited to take me out for a short ride in his new car. I gleefully agreed – knowing nothing about what he was about to do to my future aspirations of having disposable income.
After jumping in and cruising gently out of the carpark to a quiet T-junction; Chris calmly proceeded to slam his foot on the accelerator - violently introducing me to the world of TVR. If you don’t know this car, it is very quick and VERY loud. I was hooked - Cheers Chris!
A month or two after buying my own (completely standard and far too quiet) 1997 450 Chimaera, I had already visited Tim for the first time to pick up a set of his beautiful stainless, de-catted sports manifolds and a full stainless cherry-bomb exhaust together with the obligatory induction kit and carbon trumpets in order to get the noise that I so craved. There has been a fairly steady flow of projects, plans and large injections of cash ever since, always needing to make the car just a little bit faster/prettier/better; I love modifying it almost as much as I like driving it, despite quite often having very little idea what I’m doing when I set out.

Around 8 years ago, I decided that I should probably make something of a plan of how I was going to modify the car to avoid doing things in the wrong order or altering things that might not be compatible with future plans. Knowing that I would definitely want to make more changes to the engine, I knew I would need to have the ECU re-mapped at some point to give the engine the extra fuel it would need. At the time there seemed to be two options; re-map the standard Lucas 14CUX ECU via Mark Adams each time I changed something at quite a high cost (and at the mercy of Mark’s famously busy schedule), or replace the ECU with something more modern which could be adjusted by any engine tuner worth his salt (more on this later).
After doing quite a lot of research into the costs and various aftermarket ECU offerings on the market, I opted for the (then) new and popular Emerald K3 ECU – a great and well-priced piece of kit which among several other things had an excellent and easy to use software interface; the nerdy engineer within me particularly liked this as I could see and learn exactly what was going on and how the whole thing worked - even tweak the fuel map myself to my liking. So after asking lots of questions on the Pistonheads forums, studying the manuals and the Steve Heath bible, I rather naively ordered all of the bits and then commenced the disassembly of my pride and joy with a detailed step by step plan that I’d written with an estimate to finish the job in a couple of days – how hard could it be?
About 4-6 weeks later I managed to get the engine to start - luckily for me my naivety was outweighed by a steely determination - I shall leave out the details of the debacle and process of finding out that the new cam had been installed 14 degrees out of time by a reputable garage. Finally however it was time to trailer the car up to Norfolk for setting up on the rolling road by Emerald – they did a lovely job and all was good. This is when everyone on the forums or at car meets says that they live happily ever after and the car is perfect. These stories are most definitely lies.
Fast forward 7 years and I think I have had the car on dynos around 6 or 7 more times at a cost of probably £300 a go. Some of these visits have been to address areas of the map which don’t feel right after running the car for a while, or some were to re-tune to cater for new engine modifications. Some were to try and diagnose issues with the engine (usually after me fiddling). I noticed a few things through this experience:
        No one can map a car in a day. There is a reason that car manufacturers spend months on this process, and test in all sorts of temperatures and conditions (especially out on the open road).
        There are so many variables in an ECU map, and all of them have an effect on the way a car drives, or the ability to start when cold or hot, or the ability to not produce a very subtle shunt at 74 miles per hour on a very specific piece of downhill motorway when the weather’s cold.
        The map can completely change the character of the car; I also noticed that different mappers can imprint different characteristics in terms of the response and feel, and getting it wrong can make you absolutely hate driving the car. Put simply, it is just as critical as having the suspension set up correctly – probably even more so.


Last year I was driving the car one day and for seemingly no reason, the car started running strangely – it would cruise very lean, then idle very rich and generally sound rather poorly. Plugging in my trusty laptop and firing up the software revealed that nothing was amiss; all sensors seemed to be reading ok, but things weren’t running well at all. Calls to various specialists were made, tests were done and heads were scratched and the problem didn’t reveal itself – a suggestion was made to have it put on the dyno to do some more tests for another £300, plus whatever extra labour might be required to remedy the issue. That was it; there must be a better way of doing this.
Having heard about his reputation many times within the TVR world, but never actually managing to speak with him, I decided to try calling Mark Adams. I have met all kinds of characters in the TVR tuning world, and I can safely say that Mark is the most accommodating and most friendly of them all. What an absolute gentleman. Being at the end of my tether with ECUs, and being a mechanical engineer by trade, I asked Mark to run me through all options including severe engineering detail. Over the next 4 hours on the phone, he walked me though the reasons behind the drawbacks of aftermarket ECUs, and the limitations of the standard Lucas 14CUX, and various options on the market right up to the extremely expensive offerings from the likes of Motec and others. None of them he explained; come close to the capabilities of the 1994 Lucas-Sagem GEMS ECU. I was sceptical but intrigued.
The GEMS ECU is like no other ECU before or since. It was designed by Lucas-Sagem to be the OEM ECU to beat all others, and underwent a long period of design and development, with a budget of millions of pounds back in the 1990s. Utilising a dual core processor, fully waterproof and pressure sealed casing, OBD communication and extremely hard wearing design, the ECU is tough, and quick enough to do what it needs to do even when paired against modern contenders. Its special skill however is its programming – while many ECUs have a main fuel map to work from, and a few adjustment tables for things like air temperature and air fuel ratio, GEMS takes things far beyond this and has extremely complicated maps for a level of detail simply not seen in the aftermarket world, and all of these were set up and tested over a period of years attached to a Rover V8 engine. Among other things, these engines were run at conditions not achievable by a rolling road using a large and very expensive electric engine dyno which could simulate any load on the engine, they were also run in all conditions around the world in a heavy testing programme.
During this long gestation period, the engineers at Lucas-Sagem managed to bake in a level of self-learning unlike anything else before or since. As well as being able to map itself completely autonomously to a level of refinement simply not achievable by a human tuner (Mark’s own admission), the GEMS ECU can also still get the car along the road after many of its sensors have failed; its ability to keep calm and carry on despite having nearly all of its electrical arms and legs cut off is uncanny – and to the point that the driver may not even notice. It also has extremely complicated diagnostics such that it doesn’t need to go to a garage if something goes wrong – it will tell you exactly what ailments are affecting it. They should really have called it Skynet.
This then is what really attracted me to the GEMS system, having worked with a lot of ECUs over the years, Mark explained that its this uncanny ability to work against all odds, and refine itself permanently with no human intervention is why GEMS is so good. Additional benefits of this are that it is extremely economical with fuel, fully Euro 3 compliant if plumbed in in OEM guise, and can be diagnosed by any garage with an OBD computer. I decided this was the only option (particularly as my car can be tricky to map due to having a supercharger fitted), despite finding out rather alarmingly that it had never been done before on a TVR (except 2 factory specials from TVR themselves destined for the emission-crazy Switzerland). Sadly for Lucas, GEMS never made it to serious mass market due to its massive over-engineering driving the cost too high against its rival, Bosch with a cheaper and less clever alternative so it was only ever really seen in the GEMS Range Rover and a few Morgans.



So why had it never been done on a TVR before? This was my next question to Mark, and his answer centred around three main points; the cam position sensor, crank trigger and knock sensors could present quite a large pain in the arse. The latter two could be solved quite easily using some luck; the later block type used by TVR for the 4.6L engines (which my Chimaera has) was the same as used by the GEMS Range Rovers and as such has the mounting points for the two knock sensors already in the block. Happily, it also has the attachment point for the GEMS crank sensor; GEMS uses a crank trigger mounted on the flywheel (out of the way of any debris that may foul it), so the sensor is mounted on the opposite side of the engine to the starter motor.




At the time, I was swapping out the gearbox tail-housing to one with no remote gearstick linkage so that I could install a quick-shift kit, so I called John Eales – he (or V8D) are able to supply either a standard or lightened flywheel with the GEMS trigger ring mounted correctly. I went for a lightened SD1 flywheel at a very reasonable rate which arrived in a couple of days and slotted straight in with no trouble. To keep the cost down I actually went for a second hand crank trigger. It is important here to note that you need the one with spacer pads on the two mounting eyes; the part number is listed below. Being very important for engine non-explosivity, I decided to go with new Bosch knock sensors available from Mark – the original GEMS ones are actually pretty big and bulky so the Bosch ones are much slimmer design and are as a consequence, easier to fit.
At the same time as the gearbox housing was done, I had my trusted mechanical genius – Dave Batty, fit the flywheel, crank sensor, knock sensors, a GEMS Airflow meter, and also a GEMS coil-pack with leads – I got a second hand but new-looking one from Ebay with all leads – this bolts neatly behind the plenum to existing lugs in the top of the inlet manifold.
I then drove my still sick sounding Emerald brained car back home, disconnected the battery, found my super sharp wire cutters, and proceeded to chop out the entire engine wiring loom, including everything in the foot-well and the engine bay. God that was satisfying! I wish I could do it again…

For convenience, here are the parts I needed to add for my conversion with prices I paid:
Part
Part Number
Price (ea)
New/Second H
Coil Pack
ERR6269
£35
SH
Air Flow Meter
ERR5595
£35
SH
Crank Position S
ERR6357
£30
SH
Cam Position S
ERR6169
£20
N
Knock Sensors
NSC100650G
£70
N
Lambda Sensors
ERR1834
£45
N
ECU
N/A
£20
SH
Tornado Chips
N/A
£500
N

You will note that I haven’t yet mentioned the first major reason why no one has made the conversion before; the cam sensor. To add some background to the problem, while the later TVR block is the same as the GEMS engine, the front cover is not; and neither is the sump. Since the GEMS engine doesn’t have a distributor, it does not have the hole in to which it is mounted. It also uses a long-nose camshaft with a very different cam sprocket mounted to the end; the “spokes” of which are the trigger pattern for the cam position sensor mounted in a hole in the front cover just above the crank pulley. This front cover then has a different sealing arrangement with the sump below, so it would require a GEMS sump to be fitted. There are a number of problems going down this path.
     It is bloody expensive
     None of the nice, fast road camshafts available for TVRs are available in the long nose guise (or if they were then I’m sure they would be with a price hike)
     The GEMS cam sprocket uses a simplex chain, and isn’t compatible with the stronger duplex chain that TVRs commonly use for the higher revs used on the engine.
     The big off-road GEMS sump won’t fit in the TVR chassis and you can’t buy a standard one with any baffles in for track use.
As you can see then: this is not a path to be walked, and has deterred many, but being optimistic I was sure that it could be done another way. The first idea discussed with Mark was to design a bespoke sensor based on some existing components on the market which would drop into the distributor hole and translate the rotation of the camshaft up into a small rotating trigger in a sensor housing machined to emulate that of the GEMS. This was deemed perfectly feasible, but expensive and would still see a lump sticking out of the block where the distributor once was which sounded a bit ugly. This should be a neat solution.




Option 2 was to emulate the GEMS cam sprocket trigger pattern, but while still using my duplex sprocket. I bought a GEMS sprocket and compared it to my own to see if they were of a similar size and confirmed that they were the same diameter, and mounted on the same sized shaft, but had a different woodruff key position. This is very important as the trigger patter has three fat spokes and one thin, and the thin one needs to be timed correctly when it arrives at the sensor. Checking the Land Rover engine build manuals, it was fairly straightforward to find the position of the marks on each sprocket and their position at TDC, and from there the offset was calculated from one woodruff key position to the other.

About this time, Mark put me in touch with Mike Timm; a guy who had been planning a GEMS conversion for some time on his Griff, but on a much more relaxed schedule. I contacted him and we discussed the concept of a trigger disc similar to one that David Blades had built for his VEMS powered Griffith some years earlier. Mike, also an engineer had taken the measurements and knocked up a CAD drawing in no time at all and we both set upon checking the measurements independently. Satisfied that we had them correct, I popped down to my local laser cutting shop and had a few trigger discs run out in 3mm plate; look how pretty they are!

This is where things get a bit scary (for me anyway). After draining the oil and coolant, the swirl pot, coolant pipes, power steering pump, the supercharger pipework, exhaust downpipes, chassis cross-member and crank pulley, I could finally remove the front cover – there’s actually nothing hard here, it’s perfectly doable by anyone at home with a pair of axle stands, a jack, a basic tool kit and some Swarfega.

The next scary bit was to drill out a hole for the sensor itself. Luckily there is a boss already in the TVR front cover; it just needs to be drilled out - so off I trotted to Machine Mart to buy a 22mm drill bit.


Note; Holding a drill loaded with such a large drill bit gives quite an awesome sense of power – this has got to be one of the more pleasurable steps of the conversion.
After degreasing the cover in the kitchen sink, and remembering to centre punch the hole as I was taught at school, I proceeded to be amazed at how easily such a large hole can be bored into metal using a hand drill (while covering the kitchen worktop in aluminium shavings). After an extensive wash (again in the sink) I returned to the car to offer up the trigger disc and see if my sensor would fit correctly. It did not; while the position of the sensor was correct relative to the disc, the gap between the trigger disc and sensor was far too big. Through some kitchen-bench testing earlier, I had worked out that the sensor reacts correctly when it is around 1mm from the disc; in this case I reckoned I had around 5ish mm - my hopes for an easy day’s work were instantly dashed.
My first cunning plan was to add another 3mm trigger disc in front of the first to reduce the gap to around 2ish mm, when I tried this though, I found that I could no-longer re-fit the front cover; a little examination revealed that there was a small lump in the casting which I assume is there to stop the cam sprocket walking forward in older engines. This was fairly easily dealt with using my favourite new giant drill-bit, allowing me to then fit everything back together again with the extra trigger disc (now 6mm thick) – this brought the gap right down to manageable levels.



The final piece of the puzzle was to re-assemble the rest of the arrangement, deleting the distributor drive gear and replacing with a thinner washer to account for the thickness of the new trigger disc. To save anyone else time in doing this, I have had several of these discs made in 6mm thickness with washers, and I will be selling them through Mark Adams – please do get in touch with him if you would like to consider taking on one of these conversions!
With the hardware now appearing to work, I needed to fit the sensor. It needed to work first time and every time, as it is extremely difficult to access once everything is back together. So after measuring the air gap several times, I realised that adding the gasket and any sealant to the front cover when I fit it finally may affect the sensor-disc air gap by enough to make it not read correctly. So after speaking with Mark at length, I decided to opt for more of a “TVR” approach and use a - technically sound – bodge. But a bodge nonetheless. To be absolutely assured of the sensor gap being correct, I refit the front cover with gasket and strolled down to the shop to buy a bench grinder with which I ground off the mounting lug until the sensor was a perfect cylinder, creating far more mess with black plastic dust in the kitchen than the aluminium shavings – eek! The sensor was then fitted with a Sikaflex jacket and slid very tightly into the front cover until it touched the trigger wheel before being pulled back  fraction. What a neat bodge! Mark had done this on several previous GEMS engines with good results so I decided I was fine with it. As it happened, this worked flawlessly and has ever since.
After a celebratory beer or two, engine bay was re-assembled and all fluids renewed: Hardware. Done!



The next bit was the wiring loom. Because I’m perhaps slightly crazy; I was looking forward to this part as I have always enjoyed the simple logic of how circuits work and have played around with car electrics since I built a windows PC and sound system into my Ford Fiesta as an enthusiastic 18 year old.
Having played with the Chimaera wiring loom before to put in my Emerald system some years ago, I had a good working knowledge of where everything was, but it really is quite simple once you get your head around the wiring diagrams. Unfortunately though, historic Nick had cut several corners, and chopped and changed the loom over the years to add an engine start button two different aftermarket alarms, extra gauges for the supercharger and all sorts. This added to my workload significantly, so my advice here for future Nick and anyone reading this is: do not cut corners. Oh, and: write down anything you have changed which is not on the standard wiring looms! This will save quite a lot of head scratching and swearing at yourself in future years.
After speaking with Mark lots more, I learned that because the TVR and GEMS looms are both made by Land Rover, many of the connectors and wiring colours are the same for functions, so it is actually a fairly easy job to splice one to the other; that said, all Range Rover looms were for automatic vehicles, and had lots of complexity which I wouldn’t need in my car. The simplest loom to use for a starting point was that of a North American V8 Defender with a GEMS engine as the US Defenders were fitted with GEMS in order to pass emissions testing there; being American however, they all had automatic gearboxes. 



Thankfully, Mark had such a loom on his shelf new from the factory which I duly purchased and laid out on the lounge floor in what I thought was the correct shape.  Armed with the Land Rover Defender RAVE manual and lots of wiring diagrams, I began to mark up the loom (nothing was labelled), and work out what I could cut out safely in terms of gearbox control wiring, air con and things like that. It became clear about this point that due to the left hand drive affliction of US cars, and the layout of the Defender engine bay, I would struggle to make this fit in the Chimaera as it was due to the position of the battery, fusebox and lack of a firewall bulkhead (the Defender has everything in under the bonnet). Despite my best intentions of using the Land Rover loom as a base, I ended up pretty much cutting the loom to pieces and tailoring it to fit my engine bay exactly. For this reason I would recommend anyone trying this themselves to just start from scratch, it’s probably simpler. Or, if this sounds too much like a pain in the arse to you, I will be providing either measurements or my entire loom to Mark and his team to clone so that he can provide pre-made looms specifically for TVRs at varying degrees of quality (OEM/race spec) and/or completeness (he can supply wiring pre-terminated with the correct plugs if you’d like to have a go yourself).


 As you can imagine; this took AGES. And as with all wiring, there can be several hurdles along the way. After a few weeks of the odd hour here or there however, it was ready to fit and forget. Or so I thought. I thought I would be clever and install a military spec 62-pin bulkhead connector so I could easily remove the engine for future power mods. This took hours to solder up and pin test, so you can imagine the volume of the swearing when I went to connect the battery and realised (after lots of strange readings at each ECU pin) that I had held the soldering iron on one of the pins slightly too long and the insulator had melted inside one of the connectors; shorting several pins together. Both male and female connectors were immediately cut out and hurled into the nearest bin, and then proceeded the long task of soldering 62 pairs of wires together in order to test the car. Not a good day that one, much beer was needed to console myself.


Thankfully, my workaround worked and correct voltages were now seen at all pins. Success! Nearly.
The next point to note for anyone trying this is that GEMS learns the very first throttle position that it sees as base, and cannot adjust this base downward - only up (no idea why). Unfortunately for me, when I connected my GEMS up for the first time, I had the throttle springs removed and the throttle sat half open. The first inkling I had that this may be the case was when I started the car and it shot straight to around 4k rpm – with no silencers on the car this was *quite* a shock. Although it did start first time so I can’t complain too much! Once I re-fitted the springs and set the throttle however, the car simply would not idle and sounded terrible – this one took an age to diagnose. It was GEMS that finally told me however; on Mark’s recommendation I fitted a WIFI CAN-bus dongle to the OBD port that I’d put in, and connected this to my Ipad (not bad for 1994 technology!) where it told me lots of things about how it was running, including that it was at 60% throttle on idle – doh! Resetting this via Mark sending me a new chip in the post (as I didn’t have the proper GEMS computer to do re-set the throttle), I fired it up again and this time, the car ran like a champ.


As I had a non-standard engine, and non-standard injectors, Mark programmed on a best guess base map to start, which wasn’t bad but the car definitely sounded very rough when it was first run. Mark then told me to take it for a drive for a few miles before stopping, turning the car off for 30 seconds, and then re-starting. When switched off, GEMS looks at all proposed trims and implements them to the map for the next run. So each time you drive the car, the map will get better. It doesn’t just smooth the map out either, it can tweak ignition, fuel and a whole host of trimming maps such that it can power-tune itself each time you put your foot down. My experience was that this is amazing to witness – the first few times I put my foot down, the car would feel sluggish and muted, but each time I ran it, the sound became more crisp out of the exhaust, the response sharpened and the power grew; what an awesome piece of kit! Not only that, but all of the rough running, the lumps and bumps in the map, shunting. Each time I drove it they became smaller and smoother until now the map is better than any I have had before. True to Mark’s word, it beats a human, and will continue to monitor and re-tune every time it is driven, in any condition – even if I were to change cam or fundamental components in the engine, GEMS will sort out the map within a wide range of its base.
To say I’m pleased with it then would be an understatement; although it took time and a lot of understanding to fit to the car, it is an extremely good ECU now that it’s up and running, and I would thoroughly recommend it to anyone with a RV8. It is a fantastically capable ECU and comes in at a fraction of the cost of anything which could come close in terms of capability.


Before I wrap this up, I would like to take some time to say a very big thanks to Mark. He has been fantastic throughout and has taken far more time than I could possibly have hoped for to help me understand how everything works with regular and in-depth discussions over the phone; not always in business hours! As a small return favour to him, I have agreed to write a conversion guide in order for anyone else to be able to undertake this conversion themselves with a little more ease then I, and will have the parts produced to sort out the cam position problem. If there is enough interest then Mark may also put together a kit of parts with the installation guide, and possibly even a standard loom. If you are interested in doing this, please drop either myself or Mark an email and we can both answer any questions that you have.


So what’s next for my car? Well there are a few niggles to sort out still; while I was replacing all of the dashboard wiring, I have managed to stop the headlights working which is a bit of a problem at this time of year. I also managed to accidently cut out and break the ECU speedo box so the ECU currently doesn’t know when the car is moving and when it is not which causes GEMS to raise the idle a little high to prevent any stalling. I have a fix planned for both of these things but I have decided to wait until spring to finish them up as its far too cold to work on the car outside right now!
Beyond that, I think I might drive it for a while, but driving it is only half of the fun of owning a TVR in my opinion; there’s always the re-trim that it needs, and maybe another supercharger, and maybe a 5.x engine, and maybe a chassis refurb, and maybe a bit of paintwork, and…
Thanks for reading!
Nick Simpson

April addendum:
Since writing this article, the car was kept in hibernation over the winter period (as it was far too cold to work on outside!). I managed to find the fault with the lights; a rather embarrassing one I might add – I’d simply put the ribbon cable on the switch upside down. Which I realised only after dismantling the entire dashboard. Doh!
The speedo box ended up being a little more involved. GEMS it turns out, requires a greatly different rate of pulses from the speedo sensor than is used by the speedo gauge. For this reason I had to delve a little into the world of integrated circuits, GULP! What I came up with (with some helpful advice from an electronics engineer) is this beautiful little creation, which I’m clearly very proud of. It replaces the existing box behind the dashboard, and splits the signal provided by the sensor on the diff (which I also upgraded so it actually reads below 10mph). One output runs to the speedo, and the other to GEMS, which actually sees half the speed the car is actually travelling which neatly gets around the GEMS speed limiter that Mark warned me of. If anyone would like one of these, I’d be happy to make a few more.



Once this final problem was solved, I ran the car up to Cheltenham to at last meet Mark and have him check the map over. As previously mentioned, my car is a bit of a funny one due to the supercharger and giant injectors, so Mark wanted to see it in person to ensure GEMS was adapting correctly.



It turned out to be a good decision, as Mark almost immediately identified a broken throttle position sensor; he still has no idea how the car drove so well without it working! Luckily he had a spare in the car so we changed that out and got the car running on the rollers. Expecting a full day as per usual, I stocked up on biscuits and drinks and brimmed the tank, expecting to have to again before the day was done. How wrong I was though… Once set up with a couple of ancient laptops used to talk to the GEMS chip directly (which was hugely impressive to watch by the way), Mark set about a very short tuning session. He simply scaled GEMS’s map to cover the injector range, tweaked the idle and some of the ECU’s targets before moving onto power runs. It was all over in a couple of hours and less than ¼ tank of fuel – a definite first for me at a rolling road!
Unfortunately the dyno only read up to 300bhp, which thankfully the car reached comfortably - even with wheelspin despite myself sat on the back, a boot full of weights, a driver and a passenger helping on the friction front! What we did learn though was that the power curve is just about a dead straight line, and that the car absolutely sang all the way through. An unbelievable result; the car is now immensely smooth through any driving condition, very, very predictable and all around an absolute joy to drive.
It’s been a long old road to get here, but I don’t think I’ve ever enjoyed driving the car as much as I have now – I can definitively say that it drives much better than OEM, which was the original point of doing all of this.


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